A minőségirányítási rendszer fejlesztése egy autóipari gyárban

Keywords: Testing cell, scrap removal sístem, space utilization, ergonomics, production efficiency, statistical modeling, lean methods

Abstract

My article presents the development of the HCP3 testing cell used at an automotive supplier company, aimed at increasing the production area, optimizing workflows, and reducing the scrap rate. The physical redesing of the cell, together with ergonomic improvements and the implementation of an automatic scrap removal sístem, signifocantly improved productivity, reduced the proportion of defective products, and increased employee satis­faction. As a result of these developments, both the production capacity and the effeiciency of the processes increased substantially.

References

Nyárádi, A.–Kocsi, B.–Tornyos, I.–Budai, I. (2016): Optimization of automotive industry’s manufacturing process with lean tools. International Journal Of Engineering And Management Sciences (Ijems), 1., (2.).

Ndlovu, I.–Gupta, K. (2025): Ergonomics interventions in automotive manufacturing. Engineering Proceedings,

Budai István– Pápai Máté (2024): Autóipari gyártócella kapacitáselmézése és fejlesztése minőségügyi problémák megoldásán keresztül. DE Műszaki Kar.

Nyárádi, A.–Kocsi, B.–Tornyos, I.–Budai, I. (2016): Optimization of automotive industry’s manufacturing process with lean tools. International Journal Of Engineering And Management Sciences (Ijems), 1., (2.).

Bangert M. (2024): Design of Experiments in production optimization. Quality Magazine,

Published
2026-01-22
How to Cite
BirkásK. (2026). A minőségirányítási rendszer fejlesztése egy autóipari gyárban. Dunakavics, 14(1), 17-28. https://doi.org/10.63684/dk.2026.01.02
Section
Cikkek